mg_sxviper
New member
Problem started back in Feb, on a ride, came to a stop and it was backfiring and barely running. Towed it back home, checked compression and #3 dead. Pulled the head and looked like part of a ring broke off and grenaded the piston, cylinder & head. Decided to do a full rebuild, tore all the way down, pulled the crank and didn't find any fragments in the bottom end, installed new crank seals. Replaced cyl #3 & head, new top end rebuild from mcbperformance for all 3 cylinders, torqued cylinders and head to spec. Since the snow is now gone, I can't take it on a ride. TORS is bypassed. It starts right up and I varied RPM from idle to 3500 until heat exchangers warmed up. Let cool down and repeated a few times.
It runs smooth off idle but when comes back down to idle it is visually a little rough, occasional miss (every 10 sec or so) and backfire (once in 5 minutes). Can't tell which cylinder. I can pull each plug wire and it idles down to 1400 (from 1800), the same on each so they seem balanced. Checked temp of each cylinder and all match. Can rev back up to 3000 and it's smooth. Then new plug caps and plugs, no change. What worries me is that I've never heard it backfire before until the breakdown in Feb. I have not gone through carbs again as I did carb kit on all 3 last summer and only run 92 non-ethanol.
Am I down to carburation or could it be something mechanical I missed?
Have not checked power valve gap yet, could this cause it? I did totally clean them during the rebuild.
Thank you for any help.
It runs smooth off idle but when comes back down to idle it is visually a little rough, occasional miss (every 10 sec or so) and backfire (once in 5 minutes). Can't tell which cylinder. I can pull each plug wire and it idles down to 1400 (from 1800), the same on each so they seem balanced. Checked temp of each cylinder and all match. Can rev back up to 3000 and it's smooth. Then new plug caps and plugs, no change. What worries me is that I've never heard it backfire before until the breakdown in Feb. I have not gone through carbs again as I did carb kit on all 3 last summer and only run 92 non-ethanol.
Am I down to carburation or could it be something mechanical I missed?
Have not checked power valve gap yet, could this cause it? I did totally clean them during the rebuild.
Thank you for any help.