Backwoods M Max
New member
The sno scoot that my father in law picked up for my son a few years ago really has me stumped. 2 Winters ago when it came home we managed to get it running and rode it around a little. It was after that and this winter with my son being almost 2 we tried to get it going. I had bought a bunch of parts from freedom cycle to tune it up and now it's running but I'm really at a loss.
We changed all the gas line and put a proper in tank filter in it. It had a wire screen clunk and external filter before. The hose had rotted off at the grommet for the gas line inside the tank. I cleaned the carb took it down as far as a could and gave it a nice bath in chem dip. The main jet seemed fine, the pilot jet was very gunked up and the idle air screw was at 2 3/4 turns. I was able to get the idle jet and main jet out but the nozzle is stuck. someone already tried to get it out and ground off the slot with a bad screwdriver tip so it's stuck for good. I sandblasted and cleaned up the spark plug and ran it for a little while and it started doing what it did before, spitting gas out the muffler. In the past someone tightened the idle needle so much it tried to extrude the tip through the seat so I didn't know what was going on and I just cleaned the carb again. I took it all down, gave it another chem dip bath and put it back together. Float heigh is 15mm (basically parallel to the bowl seat when you flip it upside down). That's just with the weight of the float against the spring plunger in the needle. Is that wrong? The needle/seat set look good no groove in it but maybe it needs changing anyways. Is there a viton needle tip available for these things? I went through the carb and got all the belt dust out of there and rebuilt the primary with new rollers.
I started it up and checked the idle rpm with the inductive pickup on my multi meter and it was around 2250 with the screw set to max idle speed. I'm running the air idle screw at 1/2 turn since the tip is so thin now from being over tightened. I could feel the clutch grabbing just around 4000 on the meter so that's right. I jumped on it and zipped down the driveway. It didn't want to accelerate at first and at the other end it wanted to die unless I would keep blipping the throttle. i came back and pulled the plug and it was jet black after 5 minutes of running. I'm really at a loss with this thing. I'll pull compression tomorrow just to see what it is, I haven't pulled the reeds yet to look at them. It's kind of in limbo as to who's it really is. It was bought for my son but with the intention of it staying at his house most of the time. I do most of the wrenching though so ultimately I see myself doing the work on it.
We changed all the gas line and put a proper in tank filter in it. It had a wire screen clunk and external filter before. The hose had rotted off at the grommet for the gas line inside the tank. I cleaned the carb took it down as far as a could and gave it a nice bath in chem dip. The main jet seemed fine, the pilot jet was very gunked up and the idle air screw was at 2 3/4 turns. I was able to get the idle jet and main jet out but the nozzle is stuck. someone already tried to get it out and ground off the slot with a bad screwdriver tip so it's stuck for good. I sandblasted and cleaned up the spark plug and ran it for a little while and it started doing what it did before, spitting gas out the muffler. In the past someone tightened the idle needle so much it tried to extrude the tip through the seat so I didn't know what was going on and I just cleaned the carb again. I took it all down, gave it another chem dip bath and put it back together. Float heigh is 15mm (basically parallel to the bowl seat when you flip it upside down). That's just with the weight of the float against the spring plunger in the needle. Is that wrong? The needle/seat set look good no groove in it but maybe it needs changing anyways. Is there a viton needle tip available for these things? I went through the carb and got all the belt dust out of there and rebuilt the primary with new rollers.
I started it up and checked the idle rpm with the inductive pickup on my multi meter and it was around 2250 with the screw set to max idle speed. I'm running the air idle screw at 1/2 turn since the tip is so thin now from being over tightened. I could feel the clutch grabbing just around 4000 on the meter so that's right. I jumped on it and zipped down the driveway. It didn't want to accelerate at first and at the other end it wanted to die unless I would keep blipping the throttle. i came back and pulled the plug and it was jet black after 5 minutes of running. I'm really at a loss with this thing. I'll pull compression tomorrow just to see what it is, I haven't pulled the reeds yet to look at them. It's kind of in limbo as to who's it really is. It was bought for my son but with the intention of it staying at his house most of the time. I do most of the wrenching though so ultimately I see myself doing the work on it.