buckman840
New member
I switched from my aftermarket pipe to PSI to a stock one and blew up the PTO side. The piston was melted pretty good but the other one looks pretty good. It ran for a little(~30 min) while somewhat wierd but then realized that I was in trouble too late. The fan belt was off of the main drive pulley when I started investigating the problem. Not sure when this came off causing all of my problems or at the end!?!
The PSI pipe was on the machine originally from when I bought it last year. Then I found a used stock one to avoid the tickets in WI when I make trips up there. Not sure about other preformance mods(jetting etc) at this point. Will check out as it is taken apart.
Assuming that the belt was ok when I first started could the muffler change caused the problem solely?
The PSI pipe was on the machine originally from when I bought it last year. Then I found a used stock one to avoid the tickets in WI when I make trips up there. Not sure about other preformance mods(jetting etc) at this point. Will check out as it is taken apart.
Assuming that the belt was ok when I first started could the muffler change caused the problem solely?
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