corcan1
New member
thanks for all the posts everyone, and Sideshowbob, i will be ordering the new needles and boots.
now....
i took the sled out today for some test runs with the new rebuild.
took it real easy on her, 1/4 to 1/2 throttle. brought my plug wrench with me and checked the plug color often. made a change to the needle clip to richen the mix a little and the plug color changed to a light brown (was much lighter before this change).
drove around a little longer then started to head back to my truck.
3/4 throttle for a little ways then BANG.. it happened again!
loss of power and change of engine noise... this time i hit the killswitch right away. rolled to a stop. pulled the plugs and the PTO side was white/grey.
towed it to the truck and brought it home.
took head off and saw a very whitish piston...... with a little melt near the exhaust port.
pulled the jug off and WHOA!!! bottom of the piston skirt is missing!!!!!!! exhaust side.
now. it would seem i'm having bad luck with this engine.
i did use used parts for the top end... i did not measure to see if they were worn too much. and i'm guessing they were as what else would cause the bottom of the piston to break off.
the magneto side piston, you could wiggle it in the cyl quite a bit before we took the cyl off. my nephew noticed this as he was helping me remove the topend. he believes there was too much slack and that caused the piston failure.
i am open to all suggestions.
currently, my plan is to buy a piston kit from royal, probably 0.20 and get the cyl's bored to match the new pistons. also buy the newer needles and 2 new boots off a 91 exciter as suggested above.
2 pic's of the damage. cyl's look fine!
there is about an hour run time on this engine since installed.
now....
i took the sled out today for some test runs with the new rebuild.
took it real easy on her, 1/4 to 1/2 throttle. brought my plug wrench with me and checked the plug color often. made a change to the needle clip to richen the mix a little and the plug color changed to a light brown (was much lighter before this change).
drove around a little longer then started to head back to my truck.
3/4 throttle for a little ways then BANG.. it happened again!
loss of power and change of engine noise... this time i hit the killswitch right away. rolled to a stop. pulled the plugs and the PTO side was white/grey.
towed it to the truck and brought it home.
took head off and saw a very whitish piston...... with a little melt near the exhaust port.
pulled the jug off and WHOA!!! bottom of the piston skirt is missing!!!!!!! exhaust side.
now. it would seem i'm having bad luck with this engine.
i did use used parts for the top end... i did not measure to see if they were worn too much. and i'm guessing they were as what else would cause the bottom of the piston to break off.
the magneto side piston, you could wiggle it in the cyl quite a bit before we took the cyl off. my nephew noticed this as he was helping me remove the topend. he believes there was too much slack and that caused the piston failure.
i am open to all suggestions.
currently, my plan is to buy a piston kit from royal, probably 0.20 and get the cyl's bored to match the new pistons. also buy the newer needles and 2 new boots off a 91 exciter as suggested above.
2 pic's of the damage. cyl's look fine!
there is about an hour run time on this engine since installed.


Last edited: