I've put on 100 miles so far this year and 99 srx700 was running perfect, then all of the sudden it just lost power and bogged. I was 1/2 mile from my house so i limped it back.
*Fixed a PV pullthrough in the offseason, set the freeplay via the tech faq on this site.
*Compression seems fine at 120-125 all 3. Plugs were new this season and look fine. I took off the seat and checked for air in the coolant, didn't find any air. No signs of overheating that I can tell. Brand new gas in the tank, it ran fine for the 100miles on the stabil treated gas from last season.
* carbs very clean. The main jet i can see they're all clean, the pilot i spray through and it comes spraying out the jet in the front and next to the main and out the air screw (when I have that pulled).
* Pulled up the set of wires that run under the motor back by tying a rope to one end and pulling it far out the carb side and found rub through on 3 of the wires and the tan wire was severed right where the set of wires routes under the water pump. So i think I found my problem, wipe it clean, fix all the wires. I warm the machine up, it idles fine (although the even when it first bogged it still idled fine). The tach, tach backlight, and fuel gauge start working for the first time (bought it last season). I take it easy to warm it up. As soon as I give it full throttle it bogs again.
*Most of the wiring exposed and electrical tape off and I can't find any more rub through. Up by the handlebars looks good, where it goes by the tank near the CDI.... I can't find any issues.
* Headlights work strong, no sign of any stator issue. Could the CDI be fried? Please help! thanks in advance
edit:
Threw 3 new ngk br9ecs in. Thought it might have been malfunctionting PV system, but removed pvs and it still does it.
Took the carbs apart again and each cylinder's carb has 50ml of gas when I drain it. the main jet looks fine as does its shaft and needle as i shined a light through the carb and could see its clean. the pilot jet looks fine, i can see a stream of carb fluid come out both the carb bore and the front. Needle valve looks good.
I unplugged the headlight to see if it was a weak stator. pulled the wiring back out and checked for more rub through but it looks like it was just that one section by the water pump hose.
The symptoms are that it starts, idles, does not have any power above half throttle, 0-50% works as it should, though it doesn't sound as perfect as it did before. As I get to full throttle it just loses power and never goes above 7000-7500rpm. at full throttle it goes back to 6500.
*Fixed a PV pullthrough in the offseason, set the freeplay via the tech faq on this site.
*Compression seems fine at 120-125 all 3. Plugs were new this season and look fine. I took off the seat and checked for air in the coolant, didn't find any air. No signs of overheating that I can tell. Brand new gas in the tank, it ran fine for the 100miles on the stabil treated gas from last season.
* carbs very clean. The main jet i can see they're all clean, the pilot i spray through and it comes spraying out the jet in the front and next to the main and out the air screw (when I have that pulled).
* Pulled up the set of wires that run under the motor back by tying a rope to one end and pulling it far out the carb side and found rub through on 3 of the wires and the tan wire was severed right where the set of wires routes under the water pump. So i think I found my problem, wipe it clean, fix all the wires. I warm the machine up, it idles fine (although the even when it first bogged it still idled fine). The tach, tach backlight, and fuel gauge start working for the first time (bought it last season). I take it easy to warm it up. As soon as I give it full throttle it bogs again.
*Most of the wiring exposed and electrical tape off and I can't find any more rub through. Up by the handlebars looks good, where it goes by the tank near the CDI.... I can't find any issues.
* Headlights work strong, no sign of any stator issue. Could the CDI be fried? Please help! thanks in advance
edit:
Threw 3 new ngk br9ecs in. Thought it might have been malfunctionting PV system, but removed pvs and it still does it.
Took the carbs apart again and each cylinder's carb has 50ml of gas when I drain it. the main jet looks fine as does its shaft and needle as i shined a light through the carb and could see its clean. the pilot jet looks fine, i can see a stream of carb fluid come out both the carb bore and the front. Needle valve looks good.
I unplugged the headlight to see if it was a weak stator. pulled the wiring back out and checked for more rub through but it looks like it was just that one section by the water pump hose.
The symptoms are that it starts, idles, does not have any power above half throttle, 0-50% works as it should, though it doesn't sound as perfect as it did before. As I get to full throttle it just loses power and never goes above 7000-7500rpm. at full throttle it goes back to 6500.
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