EotS1
Member
The last ride of my 01 SXR600 Redhead Triple ended badly. We rode about 150 miles Friday and Saturday, and in the last two miles before I got home things went South.
First, I noticed what sounded like a ringing sound in the motor. Shortly after, I was experiencing power loss and backfiring. I did get some of the normal "bang" backfiring, but also heard several of what I can only describe as low-frequency backfires. It's like they're almost below the frequency of human hearing, you feel / sense them as a thump.
I had noticed the sled doing that perhaps three times throughout the Winter. Other than that, it performed flawlessly.
Anyway, back to the last ride: I limped home at about 10 mph just to try and salvage what I could. When I'd try to give it any gas beyond that, it would backfire and bog.
Today, I went to step one: Just wanted to check the compression. I was sure that I would find one cylinder shot... But nope. They measured (starting with the clutch side) 107, 107, 110.
I did notice that the boot had come loose from the airbox to the clutch-side carb. I'm pretty sure that couldn't cause such issues.
Any thoughts on what's next?
First, I noticed what sounded like a ringing sound in the motor. Shortly after, I was experiencing power loss and backfiring. I did get some of the normal "bang" backfiring, but also heard several of what I can only describe as low-frequency backfires. It's like they're almost below the frequency of human hearing, you feel / sense them as a thump.
I had noticed the sled doing that perhaps three times throughout the Winter. Other than that, it performed flawlessly.
Anyway, back to the last ride: I limped home at about 10 mph just to try and salvage what I could. When I'd try to give it any gas beyond that, it would backfire and bog.
Today, I went to step one: Just wanted to check the compression. I was sure that I would find one cylinder shot... But nope. They measured (starting with the clutch side) 107, 107, 110.
I did notice that the boot had come loose from the airbox to the clutch-side carb. I'm pretty sure that couldn't cause such issues.
Any thoughts on what's next?