rechecked the tps and found it to be out of adjustment. it was at .56 volts and I adjusted to .64 volts.
I went to the races this weekend and switched the cdi with a buddies. this made no difference, the machine still fell off. I switched to my cdi and adjusted he clutching by adding a shallower helix and silver spring. the machine pulled a steady 8500 after this adjustment. Trouble is, this is just a band aid to raise the rpm.
Surprisingly, all the planets lined up and I took 2nd in 700 imp. 2 machines red lighted in the final and I was left with 2nd. LOL
Has anyone ever found issues with the stock silencer plugging off, or loose baffles etc.? When I bought this machine, it had a silencer on it that I sold, because it was too loud and I felt the stock silencer worked better. I wish I had kept this so I could try it again.